As I recently wrote, we encountered a “P0757-2-3 SOLENOID” code in our 2012 Jeep Wrangler Rubicon Unlimited (JK) on a trip. This came with a refusal to shift out of 2nd or 3rd gear, and eventually a check engine light. The service data instructions say to check all the wires between the TCM and the transmission for open or short, as well as the resistance of the solenoid coil in question. If all of those check out good (which they did), then replace the TCM. I did that and the problem returned.
As I mentioned before, the problem seemed to originally manifest when I hit a bump in the road. While testing the “new” TCM, the same thing happened: the error state occurred right after a bump in the road. Pulling over and resetting codes fixed the problem, and then it manifested again on the next bump. While this could be an intermittent fault in the solenoid coil itself, I was starting to suspect the wiring again.
Even though I tried testing for open and short-to-another-circuit conditions on the wiring harness while jiggling the wires, I was unable to find any sort of problem. Service data does not provide a very clear routing of the wiring harness, and zooming in the grainy picture seemed to indicate that the harness left the kick panel under the steering wheel (where the TCM is) and punched through the transmission tunnel on top of the transmission itself. However, that’s not the case – it goes into the main engine harness, through the firewall into the engine bay, and then down alongside the bell housing. Checking for issues in this area, I found the probable culprit.
The C100/C106 connector normally resides right next to the battery in the stock location and has the transmission control/monitor wires in it. Since I had installed the MORE dual battery tray years ago, that harness no longer had a good place to sit and was sort of laying next to the battery. Over time, the factory plastic loom has disintegrated from the heat, exposing the wires directly and also allowing the harness to slip down between the battery tray and the engine head. It was here I caught a clear view of the problem: the wires had been pinched and their insulation destroyed.
One of the conditions for setting the P0757 code is “shorted to another circuit” which really means “shorted to something other than ground”. The big yellow wire in the front of the above frayed bundle is a 12AWG ignition power circuit. In addition, several others had bare copper exposed, including the LightGreen/Yellow(stripe) wire, which is the 2-3 solenoid circuit:
It seems clear to me that being pinched where it was, the wires were not quite in contact with each other, but close. As soon as I hit a good enough bump, the engine would rock against the bundle and squeeze the wires together, causing the fault condition.
I separated the wiring harness a little further so I could re-route it, repaired all the wires that had been exposed, wrapped them in fresh loom, and bundled everything back up. It can now be secured to the battery tray well above the valve cover, out of harm’s way so hopefully that won’t happen again. Obviously my fault for not securing this well enough when the original mod was made, but at the time the loom was healthy and it seemed to stay well out of the way on its own.
We recently had something weird happen with our 2012 Jeep Wrangler Rubicon (JK), and I figured I better document the symptom and fix for posterity. We have the WA580/NAG1 5-speed auto transmission and the 3.6L Pentastar engine.
The first symptom may be unrelated, but it seems like too much of a coincidence to omit. We started the vehicle to drive home and noticed that the front power windows were entirely non-responsive. The rears worked fine, but the fronts were totally dead, like a fuse was out. As we drove, we also noticed that the transmission wasn’t shifting out of 2nd or 3rd gear (it was hard to tell without a reader) and it would not respond to an attempt to manually shift. We pulled over, power cycled the car, and everything seemed back to normal.
As we were driving home we suddenly got a check engine light and the instrument cluster went dim (as it does). This seemed to correlate to a moderate bump in the road, but it’s hard to say for sure. We again noted that the transmission seemed stuck in 2nd or 3rd gear (i.e. limp mode).
Once we got it into the garage, I checked for trouble codes and found a P0757 which identifies in a generic reader as “Shift Solenoid ‘B’ Stuck On”. However, the Jeep-specific code reads as “P0757-2-3 SOLENOID”. Basically, something wrong with the transmission solenoid responsible for triggering the shift from 2nd gear to 3rd. I followed the service data procedure for diagnosis, which involved checking the wiring between the Transmission Control Module (TCM) and the solenoid pack in the transmission, as well as checking the resistance of the 2-3 solenoid coil. That all checked out (5 ohms exactly for the coil). Service data called for replacing the TCM under those circumstances because the only thing left is the output driver in the TCM that controls that solenoid.
So, I ordered a new (to me) TCM (part number 05150729AE) from eBay and put it in. Service data says that replacing the TCM requires resetting the adaptive learning settings and re-training. I reset those (using JScan) and went for a drive. Almost immediately, it was clear that the transmission still wasn’t shifting. No check engine light (yet) but it was still in limp mode. I drove easy for a while until the transmission temperature got above the required level for the learning to start, in case it remained in limp mode until that point and then started working, but it did not.
In a parking lot I pulled codes from the TCM and found a new one: P0731 which is “P0731-GEAR RATIO ERROR IN 1ST”. From a quick google, it seemed that most people get this when they re-gear and don’t update the gear ratio in the ECU. I thought maybe this new TCM doesn’t know our gear ratio, having just been transplanted into a different vehicle (with a non-standard ratio), and that it was thus unhappy and the error made sense.
Poking around in JScan, I saw that the gear ratio in the ECU was still set properly for our setup (4.56) and didn’t see any way to tell the TCM about the ratio. I figured maybe I’d try re-programming the ratio to the same thing, which I did. Once finished, JScan said that I needed to go run the “Initialize EGS” procedure to “transfer powertrain information to the TCM”. That seemed promising, in that it fit with my guess about needing this transplanted TCM to learn the attributes of the new vehicle.
I ran that procedure, which required me to cycle the ignition a couple times. After that, I started up and immediately had 1st gear and proper shifting afterwards. Drove around a bit and then back home without throwing any more codes or exhibiting any weird behavior.
Most people will recognize CHIRP as a desktop application, which it is. However, one of the early design points for the architecture was a clear separation between the UI and the driver model. That provides a mostly clean abstraction between the task of communicating and interpreting the memory of the radio and the presentation or user interaction. While the chirp python module is not a stable library, it’s pretty internally-consistent and doesn’t change much over time. What that means is that it’s also possible to re-use the driver code in other tooling for specific purposes.
I recently got an SPE Expert 1.3K-FA linear amplifier with the integrated antenna tuner. It’s a really nice piece of gear, and it’s very well thought-out. The ATU works differently than I was expecting though, in that you pre-tune it for basically everywhere you want to operate and it automatically tracks as the frequency changes via CAT. That means it’s constantly adjusting the ATU as you dial around, which is great, but it means that you need to have done that pre-tuning ahead of time.
In order to do that, the manual gives you a large table of “sub-band center frequencies” across all the supported bands. If you make changes to your antenna, or operate on a temporary antenna, you need to re-tune every single one of them. The OEM process consists of these steps:
Look up the next frequency in the list
Dial the radio to that frequency
Set the radio to CW or RTTY (which my radio is never in)
Press the tune button on the amp
Key the radio until the tuner finishes
Goto step 1 (until you’ve done them all)
For me, step 2 takes the most time, either typing each frequency in on the direct-entry keypad or using the dial. Multiply that procedure by the 153 center frequencies (if you do all the bands) and you can see why it takes some time.
My thought was that I can/should automate that using the infrastructure in CHIRP. So I did, and what I came up with works really nice with my setup to make a full re-tune much quicker. The tool’s fully-automated workflow looks like this:
Command the radio to the next frequency in the list, RTTY mode
Monitor the output to see that you key the radio, and when you un-key:
Switches to CW mode and sends your callsign for ID (if supported), then loops back to #1
The only the thing user has to do is hit the tune button on the amp and transmit when prompted, over and over again. It’s much faster and less work. Here’s a sample interaction:
It’s tempting to use the USB interface on the amplifier itself to fully automate this process, which is very doable. However, it’s probably most prudent to require some user interaction in order to listen for a clear frequency before tuning and, of course, monitor for problems (like a failure to achieve a suitable match, etc).
I tested this on an IC-7610, IC-7300, and IC-7200. It’s certainly possible it will run with ease on other such models, but I don’t have them handy to test with. Since this uses a bunch of control frames that are not normally used (and tested) as part of CHIRP, it’s hard to say if they will all work with other models.
If you want to check it out you can see it here. It requires the chirp python module to be installed (or be locally resident). An all-in-one binary could be made.
The Kenwood TK-8180 is my go-to preferred radio for GMRS stuff. It is a rugged radio with an excellent remote-head kit, and a nice display. It’s generally pretty easy to find them in good condition on eBay, and accessories are plentiful and compatible with a long line of Kenwood radios.
The TK-8180 (and TK-7180 VHF radio) have an excellent expansion port in the back that uses a standard DB-25 female connector, which makes it super easy to interface with. In my Jeep, I mount the remote head high above the roll bars near the roof to keep it out of the way and the body of the radio under my seat. However, I don’t want to have the mic up there, with the cable drooping in my face. Luckily the expansion jack can take mic audio and PTT signals instead of the mic jack on the head.
Even though this is rather trivial, I’m documenting the connection here for my future self, and others, as I have seen people ask about this before. I’m using a KMC-35 mic, but this should work with most any Kenwood commercial mic (keypad mics that use the serial connection will not have DTMF functionality).
I used a simple surface-mount box meant for ethernet to provide a mic jack low on the center console. If you’re familiar with (and/or your surface-mount box is marked for) T568B ethernet wiring, I kept the wire colors consistent here to make it easier. I used the software to set AUXI/O7 (pin 12) to “External PTT (Voice)” and “Active Low”. If you choose a different pin for PTT, make sure to adjust accordingly in the table below.
RJ-45 Pin
DB-25 Pin
Signal
T568B Standard Color
1
W/Orange
2
Orange
3
6
Mic Audio
W/Green
4
25
Mic Gnd
Blue
5
12
PTT
W/Blue
6
7
Gnd
Green
7
14
SB (+12v)
W/Brown
8
Brown
The TK-8180 can also tolerate both mics being connected at the same time, and the radio will route audio from the proper one depending on which PTT is pressed. This is not important for my application, but may be for others.
I have a Kenwood TM-281 that I got second-hand from an unknown source, and have always programmed it by hand since it’s so simple. Recent efforts in the chirp py3 branch require a lot of re-testing of radios, so I decided to pull out my TM-281 for a quick verify. Come to find out, it was totally dead in terms of serial communications. Neither chirp nor Kenwood’s own program would talk to the radio, and a serial terminal confirmed no communication at all.
I whipped out the schematic and traced the two serial lines from the mic connector that are required to operate. The HOOK line is used as data RX for the radio, and has a zener diode (D902) between that line and ground, presumably to clamp RS-232 level voltage to the 5v it expects. I found this diode to be shorted, failing a diode direction test and registering about 4ohms to the chassis.
Since I’m using a proper 5v TTL cable, I decided to lift one side of the diode to break the short to see if that would allow communication. Luckily, it did and the radio immediately started responding to serial commands normally. Here’s a picture of the diode lifted:
I recently installed GenRight regular aluminum front fenders on my TJ. It was my first time doing fenders and it turned out to be a lot more than I was planning for, so I thought I’d document some of my notes here for anyone else that might be wondering about the process. I’ll also include some thoughts on GenRight and the fenders in general.
First off, I called GenRight before I ordered, asking for the install instructions ahead of time. I hate when companies don’t just publish these on their site, both for pre-order information, but also because I want to maintain a PDF copy long-term and refer to that during install. They were super nice on the phone and assured me that the install was very easy if you also go with their inner fender liner (which I wanted anyway). They did email the instructions after the call, but they were the wrong ones (for the hi-fender instead of the regular). But, I figured they’d be pretty much the same, minus the cutting of the hood and ordered.
The shipment came super fast via FedEx, which was awesome. Seems like most places have a lead time measured in weeks. I was, however, not impressed that some of the pieces were missing instructions, and some had the wrong instructions included. I ended up getting all the right PDFs from them after a second call, including other things they had said would be included, like a template for trimming my existing sliders. The guy on the phone noted that “oh by the way, the instructions don’t mention that you need to find a new washer bottle because the old one won’t fit.” That was the first indication that the instructions were vastly under-documenting the process. I think that keeping the stock inner fenders would have been massively easier (although I’m glad I now have flat surfaces under the hood for mounting new things).
The other thing is, even after I got the right instructions from them, they clearly were written years ago and the actual products I received had been revised since then. I can guess at how stuff goes together as good as the next guy, but I assumed that for the price premium I’d be getting instructions that matched the stuff I ordered.
So, I’m disappointed in the instructions and lack of communication of all the details involved. Obviously I’m happy with the outcome and the quality of the actual product.
Install Notes
Don’t even bother trying to get the old fender off and the new fender on with the sliders in place. I did get one side off and did a little fitting of the new fender, but ultimately removed the sliders for most of the job. Mine are two-piece JCR sliders, so that was more work than otherwise. Also, plan to remove not only the battery tray, but also the mounting bracket (on both sides!) for initial fitment. In fact, plan to mount and un-mount pretty much everything a couple hundred times.
The template they gave me for trimming the sliders was helpful, but it wasn’t clear exactly where to line up the “TJ Firewall” line, since the firewall is a stamped piece of steel that isn’t remotely flat. I went conservative and ended up cutting multiple times for clearance. I used a plasma cutter with the slider on the vehicle and then traced that side to the other side when I had it right. My sliders had a bolt that went through the front fender, which was still in a good place to bolt through the GenRight fender, so I did that.
When fitting the fender, the front clip needs some coaxing to line up with the bolt holes. There is almost not enough clearance inside the front mounting area of the fender to even line up the bolts. I initially used a long philips screwdriver to move the front grille into place, but ended up boogering up threads. The proper procedure is to get the bolts on the front started and then move the body-side of the fender into place since you effectively have a big lever to work with at that point. Plan to use an open-ended wrench on the front bolts with 1/4 turns for ages to get them fully seated.
This was not described in the instructions, but the product page for the inner fenders mention they are “not trimmed for any specific suspension” and also “oversized for body lifts.” So I ended up cutting large chunks out of them to fit around the factory suspension mounts and to clear brake lines using a jigsaw. To do this, I first fitted the fender, jammed the inner fender into place underneath it until it mostly seats where it should, and traced the outline of what I needed to trim on the inner. After the first cut, it fits a lot better under there, but on both sides I still had to make a lot of adjustment cuts before everything cleared. I did all of this until I had it right before I did the pop rivets to permanently mount the inner to the fender.
The battery tray on both sides needs to be trimmed just a little to clear the inner fender. The battery mount mostly fits properly, but needs a little force to get it to line up with the holes that are cut in the fender for the bolts. There are no holes pre-drilled in the inner liners for those battery bolts, so I marked them from the back side and drilled them out with the whole thing off the vehicle. The cage nuts on the battery mount were finicky, so I ended up replacing those with M8 serrated flange nuts, which fit better.
The passenger side battery mount has the vacuum reservoir underneath it mounted to the fender. I drilled and mounted it sideways to the battery mount itself to avoid having to mount it to the new inner fender.
On the passenger side, the AC liquid line is very much in the way of both removing the stock fender and fitting the new inner. I was extremely hesitant to mess with this, but there was no other way. Very gentle pressure with rags in hand made enough room to clear the old fender for removal, and then bending it down to meet the new fender after the fact. Once I did, I zip-tied some fuel hose around the line to give it some protection from rubbing on the corner of the fender.
The stock air box does not have a flat bottom, so it does not easily mount to the new fender. I ended up mounting it on long 1/4-20 bolts coming up through the inner fender using the stock rubber-bushing-ed holes. 1/4-20 nuts on the underside with fender washers provide support and nuts on the inside to keep it in place work well. I used a simple angle bracket on the inside vertical face of the fender for the third bolt. This works and lets me angle the air box just enough to clear the hood (just barely) when closed. I had to remove the passenger side radiator support rod to do this, but with the new sturdy fenders, that thing was definitely just for show.
The factory fuse box bracket is easy to bend to fit the new fender and bolt into place with the factory bolts (and some M6 lock nuts).
On the driver side, I had the cruise servo, horn, washer bottle, and an auxiliary fuse box to remount. The cruise servo again was just a matter of bending the stock bracket until all three tabs could be located on the fender and bolted in. The horn is a single bolt and similarly easy.
The washer bottle was a little less easy. Mounting it underneath the brake master cylinder would be a good option for most people, but I had already relocated my axle locker pumps there. I used a Dorman 603-001 reservoir bottle, which was a decent size and just fit when mounted on top of the fender at a slight angle. I made a cheesy bracket to hold it in place and it’s fine. The two washer pumps (for the windshield and back glass) can be drilled into the bottom in opposing orientations and I haven’t seen any leaks.
I made a simple bracket for my auxiliary fuse block to keep it upright as I expect water will be streaming in past the fenders now and didn’t want it to sit in the fuse contacts long-term. The horn is a single-bolt indexed bracket which required no modification to bolt to the fender:
Horn mounted
I got the replacement LED light package from GenRight as well. I opted to avoid the diode-and-resistor arrangement to replicate the incandescent side marker behavior and simply wire up dedicated turn signals and side markers. I used three-pin WeatherPack connectors on both sides so I can separate them if I need to remove the fenders later. The wiring and these connectors are tucked up under the top corner of the fender and secured with a rubber-lined cable clamp bolted to the fender. I re-used the factory fog light plug with the “christmas tree” stuck in one of the holes in the inner fender.
Most of the above was summed up in the instructions with a succinct “simply bolt all the underhood stuff to the new fenders” statement. A bit misleading.
So in the end, I think everything went fine. Way more work than I was expecting, but not more than I was willing. I wish the instructions were available on the product website, I wish they matched the actual product, and I wish they said even as much as “you will have to custom mount everything under the hood, so beware.” I get that this is a little more like “pieces of fenders that can be assembled to a finished product” but I’d at least like to know ahead of time that nothing is pre-drilled and is a little more of a “choose your own adventure” … adventure.
Recently my Icom IC-7000 died during transmit. The result was a totally-dead appearance, which I resolved as detailed in this recent post. After repairing it with new parts, the radio powers on, but all is not well.
The radio now exhibits a strange symptom related to the Po (power output) and ALC meters. In SSB mode, pressing the mic key shows about half-scale deflection of the power meter with no modulation and regardless of the RF Power setting. This should be zero. With modulation, some meter activity over the static level could be seen, but never full deflection. Further, in FM or RTTY mode, the power meter would show about 80% deflection when RF Power was set to 100%. This should show full-scale. Lastly, in SSB mode the ALC meter would show full deflection with no modulation if the RF Power was set over about 40%, and zero if it was set under that level. ALC should mirror the modulation input, regardless of power.
At first, this seemed reminiscent of the self-oscillation problem that could occur in the 756 and 746 radios, where the RX line wasn’t fully pulled to ground during transmit, causing similar behavior with power deflection during transmit with no modulation. However, I ruled this out by looking at the current draw on the power supply. In SSB mode with no modulation, the radio would only pull an additional two amps or so, despite the meter showing about 50W output. The power draw would fluctuate as expected with voice peaks, even though the power meter did not show any activity. In FM or RTTY mode, the power supply would show about 22A draw even though the radio claimed it was putting out less than 80% power.
Another very interesting manifestation was that the radio wouldn’t drive an external tuner. Even when connected to a dummy load, the radio would kick off a tune cycle, the tuner would achieve a satisfactory result, but the radio would kick the TUNE indicator off after it was done. My guess was that the confusing power output indications to the CPU yielded a “not a good match” determination by the radio itself.
All of this led me to think that something in the power metering or ALC circuits was not right. The forward and reflected power is sampled on the PA board at the antenna connector and fed to IC960 where it is amplified and fed to the CPU on the main unit via the HFOR and HREF lines. Since the radio was showing zero SWR deflection, and since the ALC and Power meters were based on the HFOR line, I focused there.
There is a check point in the ALC signal on the main board – CP1601. I measured 1.7VDC here during transmit regardless of modulation input or the RF Power setting. This, to me, seemed to be the problem: basically a static invalid feedback signal to the CPU, which it interpreted as power output when there was none in SSB mode, and potentially less than full output in FM or RTTY mode, when there was plenty.
There are a number of capacitors and resistors around IC960 before the HFOR line leaves for the main board, which I tried to test in-circuit. However, I couldn’t get anything like reasonable values for these without taking them out.
But, there’s a 300 ohm resistor in the HFOR line, R960. I tested this in-circuit and it seemed like a dead short. To further test it, I disconnected the ribbon cables going to the main board, which should free up one side of it and measured again. Still a dead short. So, I pulled it out and replaced it with as close of a temporary resistor as I had locally: 200 ohm. To my delight, the radio started behaving normally! SSB with no modulation showed no power deflection, and modulation made it bounce as expected. RTTY and FM showed full-scale at 100% and otherwise mirrored the RF Power setting as I backed it down, as expected
After this change, I measure differing voltages at CP1601 depending on drive and power output, which is what I would expect. The radio also happily drives the tuner, and seems to measure the proper SWR when fed with 25 and 100 ohm loads. I expect it is either not achieving full output (or over-driving the PA) due to the wrong-value resistor I installed. After replacing the temporary unit with the proper value I will test power output to make sure it’s behaving properly
I have a bit of a love/hate relationship with my Icom IC-7000. I think that it’s a fantastic radio, with a ton of stuff packed into a very small size. My radio has suffered several failures over its life and has let me down at critical moments. I want to document the most recent failure for posterity, which happens below, but first I’ll cover the background. If you are not interested, skip the history and go straight to where I describe the latest failure and my analysis.
Background
In my early SOTA days, I was hauling it up to mountain peaks with me and operating in all kinds of conditions. I’ve also used it at home, for field day, and in the back country for heavy digital modes like Pactor-3 during events, most of the time with less-than-ideal makeshift antennas. It has definitely seen a lot of action, and has lived life far from the safe environment of an indoor ham shack’s desk top. I think that it packs an incredible amount of functionality and performance into a very small package, and it was definitely a front-runner in that category. That may be why it seems to have a somewhat poor reputation for being prone to failure. I don’t really fault the radio for punching above its weight class, or Icom for pushing the envelope. Like a specialty sports car, you buy it for the performance, not the reliability. In reality, if this thing died, I don’t really know what I’d replace it with; there’s really no equivalent offering today, in my opinion.
The first major issue happened while I was using it in the backcountry to provide Winlink messaging for an event, about 2012 or so. Occasionally, the radio would just go “deaf” on HF for several minutes at a time. It would be sitting there in receive mode showing background band noise (or actual signals) and then suddenly show a zero S-meter and no noise (other than internal receiver noise) for several minutes. This would persist across all bands. Then as suddenly as it went away, the receiver would come back and it would work fine for a while…until it wouldn’t again. For this, it went back to Icom, along with a detailed description of the problem and a video showing the symptoms over the course of several hours and several such events. Unfortunately, the usually-stellar Icom service center let me down on this also. They refused to watch the video and claimed that they were unable to reproduce the problem (I’m guessing because they only tested for a few minutes). They re-seated the ill-fated ribbon cables in the radio, and sent it back to me with a bill for their troubles. They also tried to argue that what I described was my own ignorance and that obviously I had some noise source in the house that was coming and going, despite the problem first manifesting hundreds of miles away, and persisting across all bands simultaneously. But alas. In general Icom service has been great and has a good reputation for being so. Despite my poor experience with one technician, I’m still an Icom fanboy.
When the radio came back from Icom, it went straight on the shelf. They couldn’t reproduce the problem, which means I couldn’t trust it. I was disappointed and frustrated with the service center, so I just moved on. At that point, I was using my Elecraft KX3 for SOTA stuff, which is, perhaps, the perfect radio for it. The IC-7000 stayed on the shelf for probably two years until I decided to get it out to play in a contest. When I tried to power it on, I got the “click-click of death” behavior. The radio wouldn’t power on, and just energized and then de-energized the internal relay when I pushed the power button. I was shocked, because I literally hadn’t powered it back on since Icom returned it to me and it seemed like they sent it back in worse shape. I tracked this down to a shorted tantalum capacitor in the head, which is a semi-well-known failure in these radios. It doesn’t seem like that would have happened while sitting on a shelf without any power for two years, but I’m not sure. I made that repair and the radio came back to life again. I still didn’t trust it, so it went back on the shelf for a couple more years.
This past year, I did field day for the first time in a while and had a blast. I wanted to use the IC-7000, but didn’t trust it so I used my IC-7200 (which is also a fantastic radio, but not really well-suited for contests). After field day, I decided to get the IC-7000 out and work some HF from home in order to put it through its paces. It held strong for hours of full-power SSB QSOs and I was starting to think that it had been exorcised of its demons. That is, until they popped out again.
The latest failure
At one point while transmitting, the radio shut off and then rebooted. Each time I would transmit, it would shut off, and then it got stuck in some sort of loop. Whenever power was applied to the DC jack, the radio would sit in what seemed like a tight reboot loop of just clicking the relay on and off (it was so fast that the screen never had a chance to come on). I took a break, let the radio sit for a while without power, and when I came back, it powered on and continued to work for some time after that. However, it was short-lived and at one point it shut off while transmitting for what would be the last time. The radio was stone dead, showing no signs of life. No relay clicking, no speaker popping, no significant power draw when plugged in, just … nothing.
Being totally not incentivized to spend more money and frustration with the Icom service center, I decided to take another shot at diagnosing the problem. The shorted capacitor in the head had been self-resolvable, after all. I found some information about the power up process that the radio goes through, which was helpful in catching a lead to the actual fault. At all times when the radio has power, the “logic unit” (i.e. the CPU module) receives the 14v input voltage through the HV line. This powers a 3.3v regulator on the logic unit itself, which powers the CPU. There is a pull-up resistor that brings the PWRK line high to the 3.3v rail from the regulator, which goes to the control head. To power the radio on, the control head brings the PWRK line to ground, which the CPU notices, and powers on the rest of the radio by energizing the main relay through a driver transistor.
Checking the PWRK signal on the head connector (pin 2), I saw that it was at about 2.0v, well below the expected 3.3v. Pulling the cover off of the logic unit, I checked the regulator and found that not only was the output low (about 2.4v right at the regulator), but the input was also about 2.7v instead of the expected 14v from the supply.
My thought was that, like the previous capacitor failure in the head, I was looking for something that is now shorted to ground, either on the high or low side of the regulator. Checking a bunch of the bypass caps on both sides, I found none that seemed to be problematic, so I thought maybe the regulator itself was faulty. I removed it (in pieces, unfortunately) and as soon as I did, the input pad was reading 14v from the supply again.
I thought I was in good shape, so I temporarily soldered a TO-220 3.3v regulator I had in my stash to see if that would solve the problem. Unfortunately, it did the exact same thing, showing the same low input and output voltages.
Still on the path of expecting something was dragging either the input or output to ground, I decided to try to isolate the logic unit from the main unit, to see whether the fault was on one or the other. I powered the logic module while disconnected from the main unit by feeding the regulator’s input directly. Sure enough, the output held at the expected 3.3v, with no voltage drop on the input side. This, I figured, meant something on the main unit was shorted. I put the logic unit back into the main unit, and again fed the logic regulator directly, expecting to see the output be pulled down. However, even seated in the main unit, the regulator behaved properly: no voltage sag on either the input or output.
At this point, I took a break, assuming the fault was in one of the main ICs, like perhaps the CPU itself and that I’d be looking at a more substantial replacement of that entire module, or worse. But, then I had the thought that if we’re really dragging the 14v from the supply down to ~3v, we would have to be pulling a lot of current through something and things should be smoking (and they weren’t). Further, the PWRK line was available on the outside of the radio, which means it really needed to be protected from over-current if something contacted the exposed pins while power was applied.
So, I started tracing the HV line to its source. The logic unit gets it from the main unit, which basically passes it straight through from the PA unit, which is where the DC supply connects to the radio. Here, the HV line is fed from the DC supply through the c line of Bus Line 1, through an RF choke (EP703) and a 4.7 ohm resistor (R723).
This, I assume, is the current-limiting resistor to prevent that always-on HV line from smoking a trace if it contacts ground. So, I found those two components on the PA board to measure them, and luckily found them on the bottom (exposed) surface by the front-loading fuse holder. The choke read zero ohms as expected, but R723 measured (in-circuit) at 52 ohms!
The thinking here is that R723 failed and is showing much higher resistance than expected. Under no load (with the logic unit disconnected), of course the HV line reads full voltage. When applied to the regulator and CPU on the logic unit, the input voltage drops too low to start the CPU and thus no response to the power button input. It’s also possible that the CPU is running, but when the power button is pressed, the low voltage and near zero current provided to the relay gives the impression that nothing is happening.
Again looking to actually solve the problem before I make a Digi-Key order, I bypassed R723 with the lowest value resistor I had on hand, which is 10 ohm. Sure enough, the radio responded to the button stimulus and powered right up!
At this point, I think I’ve resolved this latest failure. I’ve got to replace the regulator I removed (in pieces), which will be easy. Far more difficult will be replacing R723, which is smaller than a pin head. Shown here by the red arrow, pencil eraser for scale:
If that doesn’t go well, I may just formalize my bypass resistor in the circuit and call it good. I didn’t find any reports “out there” of this exact problem manifestation, so hopefully this write-up will help someone else if they suffer the same problem, or provide clues for a solution.
I have a couple of older Kenwood TM-D700 radios that I use for APRS stuff. They’re solid radios, and even have some features not present in the newer siblings, like the TM-D710. But, they don’t have integrated GPS devices, they don’t even support SmartBeaconing, and they were designed long before Bluetooth was common of course.
I recently decided to integrate a Bluetooth serial adapter directly into one, which would make it easier to use things like APRSDroid. With Bluetooth serial, APRSDroid can pretty much replace most of the APRS functionality in the radio, but using the inbuilt TNC for the actual modem part. This means a phone or tablet in range of the radio can enable rich mapping, SmartBeaconing, and messaging, without any cabling to the actual radio itself. Bluetooth-based connection is a feature of the current TH-D74 portable radio and it is extremely convenient.
Unlike the newer TM-D710 mobile, the TNC in the D700 is in the body of the radio itself, and thus that is where the Bluetooth serial module needs to go. Luckily, the front nose of the radio is plastic, and provides a good place for us to put the module so that it won’t be shielded by the rest of the case:
The red box roughly indicates the spot where the module will go. Conveniently there is a little extra space for it under the cover.
The module I used is an HC06, which is available from various places in a lot of different form factors, brands, etc. The only problem is that these modules almost universally work on TTL-style 3.3v serial. The TM-D700 has a proper RS-232 port, which works at differential 12v signalling. Thus a TTL serial converter is required, as well as a voltage divider to lower the 5v output from it to 3.3v for the Bluetooth module. The 3.3v coming from the Bluetooth module is enough to drive the RX side of the TTL level converter without issue.
So, for this to work, we’ll need to find a 5v source inside the radio to power the Bluetooth module and the TTL converter. Then we will place the TTL converter between the serial port on the radio and the serial port of the Bluetooth module. Luckily, the radio has an option slot for the VS-3 “Voice Synthesizer” module, and that module requires 5v from the radio. Since I don’t have that module installed in either of my D700s, it seems like a perfect place to grab it, especially since the radio expects to provide some amount of power (at 5v) to that module. The pins are super tiny, but you can probe them to see which one has the 5v. It’s the second one from the edge closest to the side of the radio. Pin 7 on the schematic, labeled “C5” for “Common 5v”:
There is also a ground at the other end of the blank spot for the module, which should be easy to spot. If you have a VS-3 already installed, you may need to find 5v and ground elsewhere. I grabbed mine from this area and tacked down the wires with a little hot snot to keep them from moving.
I chose a super small TTL converter, but which already had a female DE-9 connector. I removed that connector and just wired between the appropriate pins so it would fit inside the radio.
Now, the easy thing to do here is to just wire the TTL converter to pins 2, 3, and 5 on the board, as they would be if you were connecting externally to the port on the radio. However, this will present two problems. First, you won’t be able to use the serial port externally anymore to do things like program the radio or use the TNC for other purposes. Second, you won’t have any way to access the Bluetooth module’s serial port if you want to do things like change the PIN and human-readable name. However, there’s a good solution for this: hijack some of the unused pins. The schematic shows that several of the DE-9 pins are not connected (NC):
Pins 2 and 3 are the ones we eventually need to get to, and luckily pins 1 and 4 are not connected and right next to the ones we want. So, if we connect to 1 and 4, we can then use a super small loopback “dongle” in the form of a DE-9 female plug with pins 1 and 2 connected, and pins 3 and 4 connected. So, when we want Bluetooth to be operational, we can leave the plug inserted into the front of the radio to loop it through to the serial port; when we want to program the radio with a computer or use the TNC directly, we can remove it. If we need to talk directly to the Bluetooth module for programming, we can make a serial cable that runs to pins 1 and 4 instead of 2 and 3. Further, if we decide we want to have the Bluetooth module connected to the GPS connector (for read-only “Kenwood waypoint mode” operation), we can make a small cable to run from the GPS port to pins 1 and 4 of the DE-9. We can keep the connection to pin 5 (ground) all the time, so no need to account for that. Here’s what that looks like (prior to flux cleanup):
You can see the TTL converter wrapped and hot-snotted into place on the board just below the connector. There is a relatively blank spot on the board here with just some SMT buffer resistors that make a good spot for it.
Otherwise, locating the Bluetooth module is all that is required. On the top side where the TNC module and ribbon cable is located, there is room to place the module under the cover. It probably isn’t necessary to affix it, but a small dab of glue will hold it, antenna side up, in place relatively easily:
It’s not critical to wrap the connection side like I did since the cover that goes over this is plastic, but it helps to secure the wires, the voltage divider resistors, and the bottom of the board in case it comes loose.
After the radio is re-assembled, it’s time to build the loopback. Just a single female DE-9 is all you need for this. Here’s what it looks like (before covering it for safety):
Note that the D700 requires hardware flow control to be working. Since the Bluetooth module doesn’t use (or provide) this, just jumper RTS and CTS (pins 7-CTS and 8-RTS) together to tell the radio it is always “clear to send”.
The GPS connector is right next to it, so a very short connection between pins 1, 4, and 5 on the DE-9 to the GPS connector would enable waypoint mode instead of native TNC mode.
Technically, this is all you have to do to make it work. However, you probably want to change the PIN from the default (which is 1234), as well as change the name to something useful (like “TM-D700” or similar). You need to make up a serial cable, as described, that connects to pins 1 and 4 (instead of 2 and 3 by default). Once you do, you can configure a serial terminal for 9600,8n1 and type the following two commands:
AT+PIN9876 AT+NAMETM-D70
Note that the module doesn’t seem to use carriage returns or line feeds to note the end of a command (as it should), but instead, the inter-character delay timeout. So, the best thing to do is type those commands (one at a time) into something else, and then copy/paste them into the serial terminal so that they show up all at once.
And with that, you should be good to go. The Bluetooth module will turn on and off with the radio, so power it on, and pair your Android device. Then configure APRSDroid for Bluetooth, select the proper Bluetooth pairing, choose KISS mode, and enter the following TNC initialization string for the Kenwood:
KISS ON RESTART
Then when you click “Start Tracking” APRSDroid should configure the TNC to go into KISS mode and you should see some positive response (if verbose logging is enabled). Try sending a position and confirm that the radio transmits to verify proper operation.
I recently got a good deal on a condition-unknown Kenwood TK-7160H radio. This is a nice 50W VHF high-band commercial transceiver, and I figured that even if it was a little sick, it could probably be used to add support to CHIRP. Once I had a chance to check it out, I discovered that it was almost entirely deaf — but only when it was in wide (5kHz deviation) mode. In narrow (2.5kHz deviation) mode, it was fine. Everything else about the thing was on point.
I cracked the case and followed the service manual’s description of the signal path to the IF filters. They’re on the bottom side of the board as installed in the chassis, which means it’s hard to examine them directly, but their terminals are sticking up, ripe for the probing.
Sure enough, I could scope the IF signal on either side of the narrow filter, but one side of the wide filter it was clamped hard to ground. If you are looking at the radio top-down, the wide filter is the one closest to the edge of the board:
The filters each have five pins: three closely-spaced on one side which are ground, and then two on the other side far apart. The two two far-apart ones are the filter input/output pins.
I also noticed that there was some buildup on the otherwise-clean board right around the filters. This looked like crispy flux residue, but also could have been some sort of corrosion. If it was flux, it seemed likely that someone had already been in here to replace filters, potentially only the narrow one since it was healthy?
It is well-known that some radios have issues with their ceramic IF filters. Notably, Kenwood had a rash of much-too-early failures on some of the TM-D710 and TM-V71 radios which had some people worried about long-term longevity. It has been theorized that this problem is due to electromigration due to improper buffering of the filters from the DC bias used in the narrow/wide filter selection logic. Many radio manufacturers do this across many of their models and widespread deaths of all those don’t seem common enough for this to be some major oversight by the world’s leading radio manufacturers, at least in my opinion. Other theories are that Kenwood specifically got a bad batch of Toko filters within a certain manufacturing window, and these are the ones that are dying early.
Other pictures and video I have seen of this problem revealed the affected filters showing external signs of “green death” leaking out of the filter enclosure, slowly working its way out due to increased pressure. To get a look at the filters themselves I had to remove the board, which required unsoldering the antenna connector at the back:
Once that was free, the rest of the screws will release the board from the chassis. I flipped it over and immediately noticed a few things. First, the filters were different brands, indicating that likely one had been swapped out and not the other. Second, the wide one was Toko brand. Third, the wide filter was covered in white fuzz, similar to other pictures I had seen of this problem, but not the narrow one.
Since this radio is intended for Part 90 use, it is likely that someone would have repaired/replaced just the narrow filter, as wide mode would really only be useful to a ham these days. Filters are cheap, about $5 each, and they’re fairly common across these sorts of radios. I ordered three of each and figured I’d swap out the narrow filter in this guy too, since I was in there, just in case. I opted not to do the bypass cap hack job to remove the DC bias. Kenwood’s part numbers for the filters are in the service manual:
Wide: L72-0993-05
Narrow: L72-0999-05
Here’s the wide filter desoldered, and the narrow one came out right after it:
After the board was cleaned up, both new filters went back into their spots:
The hot elements are heat sinked to the chassis underneath and mated with thermal paste. I added a little more to each landing before I reassembled it to make sure nothing was thermally compromised by the dis- and re-assembly. Don’t forget to re-solder the antenna connection to the board once it is screwed back down.
After it was all back together, I checked on the service monitor and sure enough, the wide mode was working properly again. Sensitive down well below -120dBm. Before the fix, at 0dBm, I could only barely hear the modulation through the static when I held the squelch open.
There isn’t a lot of information out there (at least that I could find) about applying these filter fixes to the commercial line of radios. Most of those probably get fixed in a shop, where radios from the amateur line are more likely to get fixed by the owner. The same theory here should apply for the UHF variant (TK-7180) as well as similar models of TK-7162, TK-8162, TK-7102, TK-7108, TK-8102, TK-8108, TK-7180, and TK-8180.